July 2009 Progress report
article by: John McMillan
Having had people working hard at Toddington to get the loco
chassis ready to receive a steam-tested boiler, it is especially
disappointing to report little progress so far with work on the
boiler, due largely to quite extraordinary circumstances.
A chance telephone call to Chatham Steam in April revealed that
they were being forced to re-locate their business by the end of
the month, and after a hurried search they had settled on the old
RAF airfield near Detling, some ten miles from their old
site. Needless to say, the upheaval stopped work on just
about everything. The move was made entirely at their
expense, of course, but it doesn't reduce the frustration at the
lack of progress especially since, unusually for a restoration
project, shortage of cash for the boiler work is not a problem!
As soon as we heard that our boiler had been moved, we paid a
visit to the new site, accompanied by a list of the items we've
delivered there over the past year; thankfully everything seems to
have arrived at the new site safely. We were told that they
hadn't checked the contents of a small pile of storage bins, where
some of our studs and nuts were kept, as a swarm of bees had taken
up residence and we declined the offer to check the parts
ourselves!
The move to Detling has given us some information that will be
very useful when the boiler finally returns. When it left
Toddington, it weighed around 18 tons. Fully tubed, it's now
up to 23 tons and the superheater assembly will add a further 3
tons or so to the weight. Add in the chimney, petticoat pipe
and sundry other fittings, and we will be looking at about an extra
10 tons added to the original weight, and suitably larger cranes
for the lift on to the chassis at Toddington.
Anyway Chatham have recently re-commenced work on the boiler,
and almost immediately found a problem. The sealing rings we
had supplied for the superheater header didn't fit properly, and in
order to ensure that we had the correct solution to the problem we
made up a dummy superheater header in the workshop. A second
set of rings was machined to match this seat, then the rings were
rushed down to Kent to keep the job going. The set that
didn't fit can be re-worked and used on the opposite ends of the
main steam pipes. Imperial sizes of nuts and bolts in the
correct grade of material are now becoming so scarce and expensive
that we have decided to make a new set of dome cover nuts
ourselves; Chatham Steam will be supplying and replacing the
studs.
Every cloud has a silver lining, so they say, and the delay with
the boiler has allowed us to undertake more work on the chassis
between the frames, which we had expected to have to do with
restricted access once the boiler is back in place. We have spent
some time getting the inside eccentric rod to fit nicely, blueing
up the bearings and mating surfaces to achieve a satisfactory
fit. The resting pad for the rear boiler foot (removed last
time) has been cleaned up and is ready for repair. The fixing
holes in the chassis have been reamed to the next size up and are
ready to take new fitted bolts.
On the tender, the long job of cleaning up the underside of the
tank has continued, with the area around the water sump receiving
most attention. All the machining on the water sump casting
has now been completed, and the shut-off valve has been fitted in
place. A lapping tool had to be made in order to cut the
valve seats; the valve head is double sided and seals to a face in
the "open" and "shut" positions, avoiding the need to pack the
valve spindle. When finished, the valve head blued up nicely,
indicating a good seal. The valve controls the water outlet
from the tender so that the trap door can be opened and the filters
removed, inspected and cleaned as necessary, without the need to
drain the whole tender tank. Another outstanding job on the
sump was to machine the trap door and make the retaining mechanism;
the last task remaining is to make a set of runners for the filter
elements, and weld them in position.
Finally, it is always useful to receive advice from other
restoration groups. We had been advised of problems that can
be encountered on newly restored locomotives, when debris from work
on stays and inner firebox plate work accumulates between the stays
and on the foundation ring in the water space. If left
undisturbed, this debris can cause a hot spot to develop in the
plate work, leading to cracks forming. A quick inspection of
the foundation ring of 35006's boiler showed that all is clear.